Aircraft Accident Report: United Airlines Flight 389/Part 1
A United Ar Lines, Inc., Boeing 727-22, Flight 389 (UAL 389) was a regularly scheduled domestic passenger/cargo flight from LaGuardia Airport, New York to O'Hare International Airport, Chicago, Illinois. The aircraft had arrived at LaGuardia, on the date of the accident, following a trip from Los Angeles, California, with stops at Sacramento, California, Reno, Nevada, Denver, Colorado, and Chicago, Illinois. The flight crew of UAL 389 reported for duty at LaGuardia Airport one hour before scheduled departure where they prepared for the flight to Chicago. The stewardesses arrived with the aircraft from Chicago. Persons known to have been in contact with the crew prior to their departure from New York noticed nothing unusual about their behavior or appearance.
UAL 389 departed LaGuardia at 1952 on an Instrument Flight Rules (IFR) flight plan at FL 350 and estimated their arrival time at O'Hare to be 2127. The crew reported at FL 350 at 2011.35. At 2012 UAL 389 came under control of the Chicago Air Route Traffic Control Center (ARTCC) reporting its altitude as FL 350 and was cleared to the O'Hare Airport via Pullman VORTAC direct to the Northbrook VORTAC, direct O'Hare and to maintain FL 350. This clearance was acknowledged correctly and the crew was advised that radar contact had been established.
At 2103 the ARTCC controller cleared UAL 389 to descend to FL 240 and to "start descent now through 31" (FL 310). UAL 389 replied "... down to 240, leaving three five." At 2106 UAL 389 was cleared to continue its descent to 14,000 feet and given an altimeter setting of 29.90 inches for 0'Hare. This message was acknowledged immediately and in reply to the controller's inquiry the crew reported they were leaving FL 280 "now." At 2109 the flight was instructed to change frequencies and within the same minute reported out of FL 260 descending to fourteen thousand. This was the last altitude information received from the crew. At 2111 the flight was cleared to descend to 6,000 feet and the clearance was immediately acknowledged correctly. At 2118:35 control of the flight was passed to Chicago Approach Control (ORD). The radar target of UAL 389 was in the vicinity of the Sturgeon Intersection (intersection of the 011 radial of Chicago Heights and 076 radial of Northbrook VORTAC, 28 miles east of Northbrook VORTAC). At 2118:38 the target was observed approximately 2 miles east of the intersection. At 2119:36 the crew contacted ORD and was advised that radar contact had been established. At this time the aircraft target was 2-3 miles west of Sturgeon. UAL 389 was cleared to maintain 6,000 feet and to depart the Northbrook VORTAC on a heading of 240 degrees. The flight was advised that instrument landing system approaches were in progress on runway 14R at O'Hare and that the current O'Hare altimeter setting was 29.93. The pilot read back the altimeter setting incorrectly, the controller corrected him, and the pilot repeated it correctly. This was the last communication received from the flight and ended at 2120.03.
The USAF Air Defense Command radar system and the SAGE computer were monitoring and recording certain high altitude tracks by position, altitude, time, heading, and ground speed. The SAGE data were reviewed and showed two tracks in the area of concern at the time UAL 389 was approaching O'Hare. The first track, identified by the computer as track A039, began at 0157.8Z (2057:48) at a point approximately 17 nautical miles west of the Salem, Michigan VORTAC (83°58' West - 42°17' North) and was dropped by the computer at 87°10' West - 42°17' North at 0217.3Z (2117:24). The second track, identified as K047, was initiated at 0218.6Z (2118:36) at 87°23' West - 42°15' North, and dropped at 0222.8Z (2222:48) at 87°52' West - 42°15' North. There was no other high altitude traffic observed by ARTCC or SAGE in the area of concern at the time UAL 389 passed through it. The track over the ground, ground speed and positions observed by SAGE were compatible with the intended flight path of UAL 389, and within the normal operating envelope of the B-727. In addition to the tracking information obtained by SAGE, two height finder readings were obtained.
The first, at 0214.6Z (2114:36) indicated the target was at 16,500 feet m.s.l. The second, at 0219.9Z (2119:54) indicatedthe target was at an altitude of 2,000 feet m.s.l. This latter altitude was considered by the Air Defense Command to be accurate within outside limits of +500 or -1,000 feet (1,000-2,500 feet m.s.l.). During the time of this latter altitude reading the aircraft was in voice communication with approach control and had an altitude clearance limit of 6,000 feet m.s.l.
Several witnesses on ships and along the western shore of Lake Michigan observed a ball of fire near the surface of the lake. These witnesses placed the time of their observation at 2120. Other witnesses reported the same general sightings but the time of their observations varied from 2100 to after 2130.
The accident location was determined by plotting the center of the wreckage distribution pattern and determined to be at a point 29.6 statute miles east-northeast of O'Hare Airport in 250 feet of water. The surface of the water is approximately 576.8 feet m.s.l. The coordinates were 87°27' 56" West - 42°15' 2" North.
The aircraft was destroyed.
An examination of the company and FAA airman records of the flight personnel aboard UAL Flight 389 was conducted and the following summary of B-727 flight and ground school information on each crewmember prepared.
held an airline transport certificate #308952 with type ratings in the Douglas DC-3, DC-4, Vickers Viscount and Boeing 727 aircraft with commercial privileges in airplane multieengine land. His first-class medical certificate was dated July 26, 1965, with no Waivers noted.
|Date of birth||9/11/22|
|Duty time since last rest period||Approx. 2 hours and 30 minutes|
|Date of employment (UAL)||2/12/46|
|Total pilot time||17,142 hours|
|Total pilot-in-command in Boeing 727 equip||59 hours|
|Total time flight training in Boeing 727 equip||22 hours & 39 minutes|
|Satisfactorily completed ground training on B-727||6/7/65|
|Unsatisfactory on type rating check on B-727||7/7/65|
|Satisfactorily passed type rating check on B-727||7/12/65|
|Satisfactorily passed en route check B-727||7/19/65|
|Satisfactorily passed en route check B-727||7/21/65|
possessed airline transport certificate #l2T5469 with a type rating in Douglas DC-6/7 and commercial privileges in airplane single-engine and multi-engine land. His first-class medical certificate was dated November 13, 1964, with no waivers noted.
|Date of birth||9/6/30|
|Duty time since last rest period||Approx. 2 hours and 30 minutes|
|Date of employment (UAL)||2/27/56|
|Total pilot time||8,466 hours|
|Total First Officer time on Boeing 727 equipment||363 hours|
|Satisfactorily completed ground training Boeing 727||10/21/64|
|Satisfactorily completed Boeing 727 transition flight training - pilot second in command||11/1/64|
|Satisfactorily passed First Officer en route check B-727||3/8/65|
|Satisfactorily passed First Officer en route check B-727||4/1/65|
|Satisfactorily passed First Officer proficiency check B-727||4/7/65|
held a pilot certificate #1367502 and flight engineer certificate #1599415. He had privileges in airplane single-engine land and an instrument rating. His second-class medical certificate was dated September 18, 1964, with no waivers noted.
|Date of birth||3/26/39|
|Duty time since last rest period||Approx. 2 hours and 30 minutes|
|Date of employment||4/6/64|
|Satisfactorily completed ground training Boeing 727||12/3/64|
|Satisfactorily passed Second Officer en route check B-727||4/19/65|
|Total Second Officer time on Boeing 727 equipment||303 hours|
|Total flight time with UAL||649 hours|
|Date of birth||11/2/42|
|Date of seniority||11/25/64|
|Completed Boeing 727 training|
|Date of birth||11/1/44|
|Date of Seniority||11/25/64|
|Completed Boeing 727 training|
|Date of last recurrent training||4/5/65|
|Date of birth||12/10/44|
|Date of seniority||3/31/65|
|Completed Boeing 727 training|
N7036U, a Boeing 727-22, serial number 18328 manufactured June 3, 1965, had accumulated a total of 611 hours flying time when the accident occurred. A numbered maintenance check was performed 125 hours before the accident and a service check was completed 16 hours before the accident. An en route service inspection was conducted before takeoff from LaGuardia. During the en route inspection a check was made for lightning damage and the No. 1 tire was inspected to insure it was suitable for service. These items were checked because of verbal comments received from the deplaning crew. No lightning damage was found and the tire was found suitable for service.
There were no discrepancies written up in the log sheet by the inbound crew but there were three deferred discrepancies on the log. These involved an inoperative circuit breaker panel light, the passenger cabin air mixing valve, and reset button in the buffet. The inbound crew stated that aside from the deferred items there was nothing wrong with the air-craft. According to the aircraft logs and the inbound crew's statements the aircraft was airworthy at the time of departure from LaGuardia.
A review of the aircraft records revealed a number of pilot writeups regarding the autopilot. In summation, the complaints were that the auto-pilot was trimming for pitch attitude, but the stabilizer did not trim to make a correction. The out-of-trim light on early B-727 aircraft had a delay relay which was set for two seconds, in the circuit. If the elevator held a pitch correction signal for more than two seconds, the out-of-trim light illuminated until the stabilizer corrected for trim. None of the writeups reflected any difficulty with control of the aircraft. A total of seven pitch channel assemblies were removed to answer these pilot complaints and five of them were bench checked and found to be satisfactory. The last writeup on the autopilot was cleared at Los Angeles on August 15, 1965 and no further entries regarding it were found in the aircraft records.
The aircraft was serviced with 2,443 gallons of aviation kerosene which gave it a total of approximately 4,950 gallons of fuel aboard before taxi-out. The total aircraft weight was 123,013 pounds and the c.g. was computed to be 26.2 percent MAC, within the limits specified for this operation.
The aircraft was equipped with three Pratt and Whitney JT8D-l engines. Two of these engines were installed by the manufacturer of the aircraft and had 610 hours of operation. The No. 2 engine was installed July 5, 1965, and had operated a total of 34 hours. None of these engines had been overhauled.
All the airworthiness directives applicable to this aircraft had been complied with.
The 2200 surface weather chart prepared by the National Meteorological Center showed a quasi-stationary front extending southeastward across Lake Michigan from near Milwaukee, Wisconsin to near South Bend, Indiana.
The weather at O'Hare, reported at 2120, was an estimated ceiling of broken clouds at l0,000 feet, visibility seven miles, temperature 72°F, dew point 68°F, wind from 120 degrees at four knots, and the altimeter setting was 29.9h inches of mercury At 2100 the Glenview Naval Air Station, Glenview, Illinois, reported the weather to be an estimated ceiling of broken clouds at l0,000 feet, visibility 10 miles, temperature 74°F, dew point 70°F, and a wind from 090° at 6 knots. Thunderstorms were observed by weather radar located at the Chicago Weather Bureau forecast center but none were in the area where the accident occurred. There is no evidence available to indicate that UAL 389 flew in any thunderstorms.
The 1834 Peoria radiosonde ascent showed that the air below 23,000 feet contained alternate layers of stable and conditionally unstable air which was relatively moist at all levels. The freezing level was near 14,000 feet m.s.l.
The crew of a B-707 was flying approximately 30 miles behind UAL 389 at FL 280 as they approached Lake Michigan. The captain of the B-707 stated that the descent over the lake was made on instruments from FL 280 until they descended to 8,000-l0,000 feet where they broke out of the clouds 15-20 miles off shore. Light turbulence and areas of precipitation were encountered during the descent. The B-707 crew could see only the lights on shore when they broke out of the clouds and the captain stated that visibility was "fuzzy and unclear." The first officer said he could see the water clearly, it was hazy, and the lights on the shoreline were visible.
The terminal weather forecast for O'Hare for the period 2100-0300 called for 10,000 feet broken clouds visibility 4 miles in smoke.
The company dispatcher at LaGuardia stated that he provided no weather briefing to the captain of UAL 389, however, a self-help weather briefing board was available to the crew at LaGuardia and the dispatch representative at LaGuardia provided the crew with UAL forecasts, sequence weather reports from Service "A" circuits 8022 and 8025, copies of the John F. Kennedy, Dulles, and O'Hare forecasts, and a copy of the 1700 jet winds.
The accident occurred in dark, hazy, VFR conditions.
There were no reported discrepancies to any aids to navigation in use at the time of the accident.
The aircraft was in radio contact with Chicago Air Traffic Controllers with no reported discrepancies.
Not involved in this accident.
N7036U was equipped with a Fairchild Waste King Model 5424 flight data recorder S/N 1740 installed July 17, 1965. Service Bulletin No. 159 requiring the installation of protective plates to prevent damage to the recording medium in the event of an accident, had been accomplished. The top and side cover, recovered as one piece, and the rear cover of the recorder were the only portions recovered. None of the recording medium, an Inconel (stainless steel with high nickel content) tape has been recovered. The two portions of the recorder case were recovered in two locations within the main wreckage area.
The main wreckage area was located on September 2, 1965, and the center plotted as 87°27' 56" West - 42°15' 02" North. Several thousand pounds of floating material were recovered from the lake in the three days following the accident but little else until the discovery of the main wreckage area. Recovery operations were discontinued December 21, 1965, with approximately 82 percent of the wreckage by weight, and all occupants of the aircraft recovered.
Search and recovery operations were resumed June 17, 1966, and terminated September 25, 1966. Particular emphasis was given to the recovery of the flight recorder, the flight recorder tape, and the missing portions of the No. 3 engine. No flight recorder parts or tape were recovered during this search. One small piece of an engine case was recovered with a small section of flange mounting and case splice attached. Approximately 1,500 pounds of additional wreckage was recovered, consisting mostly of wing skin and small fuselage parts.
Included in the floating wreckage recovered in the first three days were honeycomb material from the outboard ailerons, trailing edge flaps, and spoilers, portions of the fiberglass tall cone, passenger seats, and seat cushions. The wreckage recovered from the lake bottom included the main portion of the empennage, the landing gears, portions of all entrance doors, three of the four emergency exit windows, portions of the engine cowls of all three engines, portions of the fuselage from the radome to the empennage, and portions of both wings with parts of their attached components including both wing tips. All or part of all major components including control surfaces were recovered.
Following recovery of the Nos. 1 and 2 engines and portions of No. 3, the engines were disassembled and inspected. Both Nos. 1 and 2 were relatively intact but badly damaged although the damage to No. 1 was less severe.
Examination of the No. 1 engine revealed that there were no signs on operational distress or overtemperature operation. The bearings and lubrication system showed no evidence of preimpact failure or inadequate lubrication. The turbine section had evidence of rotational rubbing on both rotating and fixed components. The front compressor drive shaft was intact and had no perceptible twisting. However, there was a measurable runout of the shaft which varied from .003 inch at the No. 4 1/2 bearing location to 1.295 inches forward of the splines. A number of compressor blades on the front and rear compressors were bent opposite the direction of rotation and there was damage on the leading edges of many compressor blades and trailing edges of many stator vanes. Damage to the trailing edge of the stator vanes was in the direction of rotation. There was no evidence of operational distress in the combustion chambers or combustion chamber inner cases. The first stage nozzle guide vanes showed little evidence of foreign object damage but there were light aluminum splatters on the vanes. The fuel manifold was pressure checked and exhibited no evidence of fuel leaks. The clamshell doors were just out of the "open," forward thrust position.
The No. 2 engine was recovered with the fan section and the first two compressor stages separated from the rest of the engine. The front accessory drive was not recovered. The recovered compressor blades of these stages were bent opposite the direction of rotation and the stators were bent and damaged in the direction of rotation. The majority of the compressor blades in the remainder of the front compressor, through the sixth stage, were bent opposite to rotation and the stators bent in the direction of rotation. There was no evidence of inadequate lubrication found in the engine. There was damage to the seventh through the twelfth stage stators on the trailing edges, in the direction of rotation. There was foreign object damage to the leading and trailing edges of the thirteenth stage stators. The compressor blades of the rear compressor were bent opposite rotation and showed some tip rub damage. There was no evidence of heat distortion or uncontrolled burning in the combustion chamber assemblies. There was no evidence of overtemperature in the nozzle guide vanes. The front compressor turbine drive shaft was separated at a point 53.5 inches from the forward face of the second stage turbine disk mounting flange. The break at an approximate 45-degree angle to the longitudinal axis of the shaft. The shaft was bent forward of the No. 4 1/2 bearing. The first three turbine stages showed minor rotational damage. There was no evidence of operational distress in the turbine section.
The fan inlet case assembly of the No. 3 engine inlet guide vanes remaining in the case were bent in the direction of rotation and six of them were broken on the hub end The front compressor front hub and blade assembly was recovered with most of the blades attached. The blades were twisted and bent opposite the direction of rotation There was no evidence of operational distress on the hub. The recovered stator vanes of the first stage were bent opposite the direction of rotation and separated from the inner support. Approximately 50 percent of the second stage compressor blades of the front compressor were bent opposite to the direction of rotation. The remainder of the blades were bent aft. The third stage compressor disk was recovered separately with three compressor blades attached. These blades were bent 20-30 degrees in a direction opposite to rotation. The face of the disk was severely rubbed.
The recovered fuel boost pumps, valves, and fuel system components showed no evidence of malfunction or operational distress. There was no evidence of fire or overpressure in the fuel system plumbing except the sooting of two pieces. One was a section of fuel dump tubing and a connector assembly with sections of tubing attached. In the fuel dump tubing, sooting was seen over deformed areas, and in the connector, an area of deformed tubing pulled away from the inside diameter of the connector was not sooted, leaving a clearly defined line corresponding to the area that is normally under the connector. Approximately 75 sections and fragments of other fuel system tubing and tank structure were recovered and exhibited no evidence of fire, explosion, or electrical arcing.
The Nos. 2 and 3 thrust reverser clam shell doors were in the (forward thrust positions), and the Nos. 2 and 3 reverser lockout actuators were in the locked position. The directional control valve rocker arm of the No. 1 engine was bent outboard and broken off. The thrust reverser followup cam was free and the directional control valve could be operated manually.
The thrust reverser control cam was in a position to have either the cam roller or the directional valve control in the reverse position. When the broken sections of the control arm were matched, the control valve was in the reverse thrust position.
Several pieces of air distribution and air conditioning ducting were recovered. This ducting was installed overhead in the fuselage area. There was no soot or fire damage on these pieces of ducting. Both engine bleed air valves were found in the open position. The components which make up the cabin pressure control were recovered. The rate of climb indicator was intact in the panel but the pointer was detached from the shaft. The differential pressure gauge was intact. The cabin altitude pointer was on 30,000 feet and the cabin differential pointer was set at approximately 6.3 psi. The automatic cabin controller was recovered intact with the cabin altitude pointer on l,OOO feet. The rate selector knob was turned to "decrease" and the barometric setting in the window was 29.29. The setting of the flight altitude and maxnmum differential in the window was between 2#,OOO-25,000 feet. The manual cabin pressure control pointer was in the center of the automatic range. Only the top covers of the two outflow valves were recovered.
The automatic pilot control panel was recovered with the mode selector switch in manual, the integrated command knob slightly left of center in the turn mode and neutral in the pitch mode, the aileron and elevator engage switches in a mid-position between "engage" and "disengage," and the altitude hold switch "off."
The automatic pilot stabilizer trim servo assembly was tested and no discrepancies were found. The left and right elevator position and trim sensors were bench-checked and found to be O.6° and 3.4° off zero, respectively.
The No. 1 VHF communications receiver and control selector were found tuned to 129.35 mcs., an ARINC (company radio} frequency for Chicago. The No. 2 VHF communication control selector was found set at 119.0 mcs., the frequency of the O'Hara Approach Control on which the flight had been communicating. The No. 2 receiver was not recovered.
The recovered wiring of the essential electrical Power panel had no evidence of overheating, arcing, or burning. Examination of the three main engine generator feed cables and the male portions of the Nos. 1 and 3 generator connectors revealed no evidence of arcing, overheating, sooting, or burning. The generator control panel switches were set for normal operation. The essential power switch was set for the No. 3 engine, normal for UAL, and the No. 3 engine bus tie relay was in the "closed" (normal) position. The two constant speed drive units recovered from the Nos. 2 and 3 engines were ﬁound in the connected position. The electrical actuator for tail skid positioning was extended approximately 3 inches which corresponds to the skid retracted position.
Examination of the flight control systems showed the aileron components were damaged with the aileron centering mechanism in neutral (centered). The aileron power control unit and linkage were intact, although broken away from the structure. The mechanical linkage was in a 5 degree left aileron down position. The power unit was separated from the mechanical unit and the broken ends of the cable strands were necked down in the area of separation. The aileron trim indicator cable drum was in the neutral position. The elevator centering spring assembly was in the center position and could be moved to contact both stops. While the elevator control linkage was damaged, there was no evidence of pre-impact distress or failure. The elevator feel computer and feel control units were functionally tested and met all test requirements. The horizontal stabilizer jackscrew was examined and the "B" dimension between the stops measured at 5-3/4 inches. This is equivalent to 0.5 units of aircraft nose up trim. The stabilizer trim brake assembly was recovered but the drive sprocket, brake release arm and mounting flanges were not recovered. The left hand stabilizer brake stop pawl and attached spring cartridge were found in an overcenter position against the case. This pawl is designed to stop stabilizer movement in the aircraft nose up direction. In this position the pawl was beyond the designed limit of its travel and could not function as a brake or stop device. The stabilizer trim brake system is actuated by operation of either pilot's control column to stop stabilizer out-of-trim motion. Should a runaway stabilizer cause a pitch in an unwanted direction, moving either pilot's control column in the opposite direction will stop the stabilizer from further movement in the out-of-trim direction, but will permit movement in the opposite direction. A measurement was taken of the control stand stabilizer trim jack assembly and 1.7 inches existed between the trunion and the nut assembly. This is equivalent to 1.25 units aircraft nose down. The hydraulic power units of the ailerons, rudder and elevators were recovered and tested. The aileron power control unit passed the functional test. During the testing of the upper rudder power units it was determined that the linear position transducer slide was not free to move resulting in an over-tolerance of the phase log test. No other discrepancies were noted. Testing of the elevator power control units showed no discrepancies except that the transducer output voltage was low and the autopilot override velocity timing was slow.
Testing of the ten flight spoiler actuators revealed that the Nos. 4 and 5 and Nos. 10 and 11 units did not pass a cold soak test. Further, the internal piston of the No. 10 actuator was broken and when power was applied the actuator went to the extended position.
The leading edge slat selector valve was recovered with the slide assembly in the retracted position and the No. 3 left hand slat actuating cylinder was found with the piston rod locked in the retract position.
The electrical stabilizer trim actuator was tested to stall torque specifications of 600-650 inch pounds in clockwise and counter clockwise directions. The unit stalled at 480 inch pounds clockwise and 456 inch pounds counter clockwise. Both the main stabilizer and autopilot cruise trim switches were found in the "on" position.
Two attitude indicators were recovered. One showed evidence of a 74-degree right bank and the other of 53-degree left bank. The second indicator showed a pitch attitude of approximately 5 degrees nose up. A master heading indicator was recovered and displayed a heading of 260 degrees on a test stand with a selected course of 251 degrees. Both automatic direction finding receivers were recovered. One was found set at approximately 390 kcs. and the other at approximately 780 kcs. The mode selector was in the loop position. A VHF navigational receiver was recovered set at 113.0 mcs., the frequency of the Northbrook VORTAC north of O'Hare Airport.
The first officer's altimeter was recovered with a barometric setting between 29.91 and 29.92. There are two three-pointer type altimeters installed in the cockpit, one on each pilot's instrument panel. These altimeters have three concentrically mounted pointers, coded in length and shape. The long pointer indicates 100's of feet, the short, stubby, roughly diamond-shaped pointer indicates 1,000's of feet, and the shortest pointer, with a short cross bar, indicates 10,000's of feet. The 100's pointer makes one complete revolution per 1,000 feet of altitude change, the 1,000's pointer makes one complete revolution per 10,000 feet of altitude change, and the 10,000's pointer makes one complete revolution per 100,000 feet of altitude change. The 10,000 feet pointer is painted on a rotating plate which has a slot cut around part of its circumference and a wedge-shaped cutout on the face of the plate approximately 90 degrees to the left of the pointer. The two cutouts are arranged so that at zero elevation the wedge exposes a black and white hash marked area and the circumferential cutout exposes a black background on the instrument face As the altimeter is taken to higher altitudes the plate rotates clockwise gradually exposing a white arc to the left of the 10,000 feet pointer and gradually covering up the hash mark area. At an altitude of approximately 16,000 feet the hash mark area is completely covered and the white arc is exposed to a point approximately halfway between the Nos. 1 and 2 on the face of the altimeter. As the altimeter is taken further up in altitude more of the white arc is exposed. As the aircraft descends the situation is reversed and the white arc is gradually covered up and at approximately 16,000 feet the hash marked area is again brought into view. For examples of altimeter presentations see Attachment #2.
The two altimeters are served by separate static sources and there is no way in which the information on one altimeter can be displayed on the other. Any error that occurs in one system cannot be displayed on the other instrument thus providing a continuing cross-check capability for the crew. A review of the aircraft records revealed no history of altimeter malfunctions or problems.
A majority of the witnesses reported an explosion and fire on or just above the horizon over Lake Michigan. Those witnesses nearest the accident, on ships in the area, reported the time of the explosion at about 2120. Several pieces of floating wreckage were recovered which exhibited smoke and soot discoloration particularly on the broken edges. While there was a fire and explosion on impact with the water, there is no evidence of a fire in flight.
Both engine fire extinguisher bottles were recovered with the discharge discs intact. Three fire extinguishers installed in the cockpit and cabin were recovered. The charging cartridge in a water type extinguisher was not discharged. A dry chemical extinguisher was still charged and a functional test revealed that it operated properly. A CO2 extinguisher was recovered in a damaged condition and could not be discharged.
This was a non-survivable accident. Pathological and toxicological examinations of the flight crew revealed no evidence of pre-impact incapacitation nor was there any evidence of foul play.
A special investigation was conducted at New York to review the pre-takeoff activities of the crew and passengers and the activities of the ground servicing personnel. No evidence was discovered which could be related to this accident.
As a part of this and other B-727 investigations a special study group reviewed the flight characteristics and applicable aerodynamic data of the B-727. One of the areas of investigation of this study was an evaluation of the pilots response to the question "have you ever experienced altimeter lag or sticking, particularly after descent from high altitude, at high rate, with aircraft cold soaked and entering weather conditions of high moisture content at the lower altitudes." The affirmative comments on altimeter sticking or jumping which were received in reply to this question were associated with altitudes above 20,000 feet. None of the pilots questioned reported any difficulty with erroneous altimeter readings at altitudes below 20,000 feet.
This group also reviewed the pilot training program with regard to information disseminated to the flight crews regarding the flight characteristics of the aircraft. The results of this study disclosed no evidence of any design or performance deficiency and pilots were generally pleased with the flight characteristics of the aircraft and they had experienced no major difficulties in the operation of the aircraft. All of the air carrier training and operations manuals reviewed stressed the fact that high rates of descent close to the surface of the earth should be avoided.
In addition to the above study, a review of Mechanical Reliability Reports on the B-727 was conducted to determine if there was any discernible trend in reports of static system problems or instrument problems traceable to the static system. No history of static systems or instrument problems was found.
Because of the failure of some of the speed brake actuators to pass a post-accident cold soak test, the history of spoiler malfunctions in the B-727 fleet was reviewed. It was found that when spoilers malfunctioned and the actuators would not pass a cold soak test, the problem appeared as a failure of some of the spoilers to extend when the speed brakes were selected to the extended position. This failure to extend resulted in unwanted rolling of the aircraft but was found to be controllable by the pilots. It was also noted that this problem only appeared at the high altitudes and was not reported at lower levels where an unwanted roll might be more hazardous.
As a part of this investigation a review of research on altimeter reading problems was conducted. There are some fifty studies relating to the various altimeter systems of presenting information to pilots which have been conducted since 1947. One of the most recent studies completed by the Naval Research Laboratory, Washington, D. C. was conducted to determine the relative effectiveness of various altimeter displays. These investigations, consisted of laboratory research at NRL and flight test at a nearby naval air facility, were in support of a Department of Defense program. Four types of altimeter presentations, the counter-pointer (CP), counter-drum-pointer (CDP), drum-pointer (DP) and three pointer (3P) were compared in a series of laboratory experiments measuring reading time and accuracy with both pilots and non-flying enlisted men. The same instruments were also compared by the pilots in flight, using the questionnaire technique to elicit pilot judgments. The results of the various phases of laboratory research showed that the three-pointer altimeter consistently ranked poorest. The pilot preference in the flight tests was overwhelmingly in favor of one of the other types of altimeter. In all objective measurements taken, the three-pointer altimeter ranked the poorest among the instruments tested. The finding that the three-pointer was poorest proved to be statistically reliable in every study in which tests of statistical significance were applied. In a preceding part of this study the mean exposure tune and number of errors on each altimeter was recorded for the two test groups, one consisting of pilots, and the other of non—pilot enlisted men. In 1080 readings of the four altimeters by 18 pilots the mean exposure time in seconds was 0.80 for the CP, 0.84 for the CDP, 1.38 for the DP, and 2.28 for the 3P. The number of reading errors was 7 for the CP, 14 for the CDP, 26 for the DP, and 80 for the 3P. The same data collected during 420 reading trials using 7 non-pilot enlisted men resulted in mean exposure times of 0.85 for the CP, 0.86 for the CDP, 1.50 for the DP, and 2.93 for the 3P. The number of errors by this group were 5 for the CP, 2 for the CDP, 10 for the DP, and 52 for the 3P. The mean number of errors made on each altimeter for pilots was 0.39 CP, 0.78 CDP, 1.44 DP, and 4.44 3P, and for enlisted men 0.71 CP, 0.29 CDP, 1.43 DP, and 7.43 3P.
- All times herein are central daylight time based on the 24-hour clock unless otherwise indicated.
- Altitudes above 17,000 feet are expressed as flight levels (FL) and reported in three digits i.e., FL 180. Flight levels are derived from a reference datum of 29.92 inches of mercury set in the altimeter as a barometric setting.
- The voice was identified as that of the captain.
- Semi-Automatic ground environment.
- Positions are recorded in latitude and longitude of an intersection which is the southwest corner of a rectangle measuring one nautical mile on a north-south axis and approximately .74 nautical mile on an east-west axis. The target may be located anywhere within this rectangle.
- While there are potential errors in the height finding data experience has shown they are to a great extent self-cancelling.
- Time is expressed in hours, minutes and tenths of minutes and expressed as Greenwish Mean Time (Z).
- "Heading" is actually the magnetic track being made good by the target.
- Ground speed is derived by continuously averaging the time vs location plot.
- All aircraft and pilot times are reported to the nearest whole hour.
- Inspections performed at no more than 525 hour intervals.
- Conducted every 125 hours.
- The dispatcher for this flight was physically located in Chicago and had a delegated representative who signed the clearance in the dispatcher's name and provided service to the crew on the dispatcher's behalf.
- Runout is measurable bending of the shaft along its longitudinal axis.
- Exhibit No. 12-A, SA—387, AAL B-727 accident near Constance, Kentucky, November 8, 1965.
- NRL Report 6242, Altimeter Display Evaluation, Final Report, Jan. 26, 1965.
- NRL Report 6232, An Experimental Evaluation of Four Types of Altimeters Using Both Pilot and Enlisted Men subject, December 18, 1964.